Near
New Albany, Indiana, just across the Ohio River from Louisville,
Kentucky, the CSX Transportation railroad rumbles six times
daily, hauling freight through the southern Indiana countryside.
Six times
a day, the railroad depends on the track to provide an unyielding,
stable foundation for the weight of its 50-mph diesel-locomotive-driven
revenue producer. Six times a day, 365 days a year, the rail
bed must not erode, and the embankments must remain rock solid.
Stone box culverts created 150 years ago and the updated
corrugated pipe brethren that followed them 70 years later channeled
the creek and field run-off water under and through the rail
bed of one five-mile stretch of this railroad as it runs north
from New Albany to Salem, Indiana. The years took their toll
however, and the rusted corrugated pipe and deteriorated stone
culverts began to collapse, requiring replacement to avoid
threat of erosion to the embankment and the rail bed. Getting
the job done with minimal disruption to train traffic was
the challenge facing CSX Transportation.
CSX
Transportation Supervisor of Bridges, Craig S. Guth, P.E.,
summed up the problem facing the railroad, "The concerns
of CSX Transportation while planning this drainage replacement
project were many." Safety concerns with settlement, quality
concerns about the track and its rail bed, and revenue-losing
disruptions to train traffic were high on the priority list. |


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There were
five drainage culverts scheduled for replacement out of the
1,100 in the 80 miles that separate Louisville, Kentucky, and
Bedford, Indiana. Originally, the railroad planners thought
that they would be forced to bid the job on an open-cut basis
and demand from the contractor that any one of the new pipes
be installed in a single day, with the trench backfilled and
compacted, and the track replaced by nightfall so trains could
be routed to run the track the same evening.
This original
plan faced potential scheduling nightmares. So when Len Liotti,
owner of Midwest Mole, Inc., suggested using pipe ramming with
a large HammerHead Mole to push in the new casing and install
the new drainage pipe without disrupting train traffic, railroad
officials were all ears.
"Pipe
ramming was the superior method for the replacement of these
drainage pipes," said Guth. "Not only were we able
to keep train traffic moving without any disruption, but we
had no fear of loss of integrity to the rail bed and embankment.
We didnt have to worry about creating any voids during
the installation since we were driving a solid steel
pipe or any post-project settlement. Despite the higher
up-front costs, it accomplished what no other method could
have."
Liotti and
his crews know about putting holes in the ground. Theyve
used a variety of tunneling methods for the past 16 years,
working with auger-boring machines, micro-tunneling, hand tunneling
and, more recently, pneumatic pipe rammers. According to Liotti,
pipe ramming has become his preferred method for culvert replacement
work. "When you have soil conditions like those underneath
these rail beds including: like boulders, cobble, sand and
gravel, rip rap and rail ties pipe ramming with the
large pneumatic tools is much better than traditional auger
boring. When we ram, the lead-reinforced pipe edge shears the
ties and cuts and breaks up the rocks. With auger boring, not
only would the boulders cause the pipe to go off line and grade,
but the rocks would get stuck in the flighting."
Two of the
five culvert replacements demonstrated the reason why Midwest
Mole, Inc. employed pipe ramming. On the first of the replacements,
the crew installed 50 feet of 36-inch pipe. Rather than punch
a new hole through the rail bed, the crew went through the
existing culvert, swallowing up the existing deteriorated 24-inch
corrugated pipe. David Miller, Midwest Moles crew foreman,
described the installation. "Because we took the casing
over the existing corrugated pipe, we were able to follow established
drainage patterns and didnt have to fill in the old line
with grout and move over for a whole new line. During the ramming
part of the job, the 16-inch HammerHead Mole hammered the 50
feet in a half hour, chewing right through old rail ties. If
we had been using any other method, those rail ties would have
stopped us cold."
The process
Midwest Moles crew used entailed getting access to adjacent
property and moving its excavation equipment and the rammers
to the site. After excavating the launch pit, they leveled
it and installed their auger-boring unit track and set it on
their desired grade. They had their pipe contractor fabricate
a reinforced soil shoe on the lead pipe so that they had quarter-inch
clearance from the bore wall on the outside of the pipe and
a quarter-inch clearance from the spoil accumulation on the
inside of the pipe. Because of the short length of the bore,
Miller and his crew did not add lubrication for the ramming.
After ramming, they cleaned out the spoil using their auger
flighting. All the restoration work was completed before the
crew moved on to the next culvert replacement.
As the crew
worked, the trains ran uninterrupted. The crew did stop the
pneumatic tool ramming once, however, so that the vibration
of a passing train would not shake the track.
Another casing
rammed in was 48-inches in diameter in order to concentrically
swallow up the deteriorated 36-inch corrugated pipe. Midwest
Mole brought in the 23-inch HammerHead Mole to hammer the half-inch
wall pipe through the 50 feet of Indiana limestone to move
the new drainage pipe through the existing culvert.
With its
48-inch adapter ring and 24-inch collets to accommodate the
tool, the HammerHead was lowered into the launch pit some 20
feet below the track surface. The tool was started up; it taper-locked
itself into the collets and the push was on.
"If
we had not pipe-rammed this culvert, we would have had to open
a new culvert, direct the creek away from the original channel
and turn the creek on the other side another 90 degrees so
they would meet up," said Liotti. "By hammering with
the pneumatic tool, we saved a lot of time and tons of rip
rap that we would have had to restore the site with." The
23-inch HammerHead pounded the 50 feet of 48-inch diameter
pipe in under 90 minutes, with most of the time spent during
the last 12 feet of the push. When the crew cleaned out the
limestone spoil, they saw the aggressive chipping accomplished
by the tool.
"With
pipe ramming we had no interruption of service," said
Guth. "So we know this is the way to go on these culvert
replacements. There was no appearance of any settlement or
any concern about rail bed or track integrity." |