Near New Albany, Indiana, just across the Ohio River from Louisville,
Kentucky, the CSX Transportation railroad rumbles six times daily,
hauling freight through the southern Indiana countryside.
Six times
a day, the railroad depends on the track to provide an unyielding,
stable foundation for the weight of its 50-mph diesel-locomotive-driven
revenue producer. Six times a day, 365 days a year, the rail
bed must not erode, and the embankments must remain rock solid.
Stone box culverts created 150 years ago - and the updated corrugated pipe brethren that followed
them 70 years later - channeled the creek and field run-off water
under and through the rail bed of one five-mile stretch of this
railroad as it runs north from New Albany to Salem, Indiana.
The years took their toll however, and the rusted corrugated
pipe and deteriorated stone culverts began to collapse, requiring
replacement to avoid threat of erosion to the embankment and
the rail bed. Getting the job done - with minimal disruption
to train traffic - was the challenge facing CSX Transportation.
CSX Transportation
Supervisor of Bridges, Craig S. Guth, P.E., summed up the problem
facing the railroad, "The concerns of CSX
Transportation while planning this drainage replacement project
were many." Safety concerns with settlement, quality concerns
about the track and its rail bed, and revenue-losing disruptions
to train traffic were high on the priority list.
There were five drainage culverts scheduled for replacement
out of the 1,100 in the 80 miles that separate Louisville, Kentucky,
and Bedford, Indiana. Originally, the railroad planners thought
that they would be forced to bid the job on an open-cut basis
and demand from the contractor that any one of the new pipes
be installed in a single day, with the trench backfilled and
compacted, and the track replaced by nightfall so trains could
be routed to run the track the same evening.
This original plan faced potential scheduling nightmares. So
when Len Liotti, owner of Midwest Mole, Inc., suggested using
pipe ramming with a large HammerHead Mole to push in the new
casing and install the new drainage pipe without disrupting train
traffic, railroad officials were all ears.
"Pipe ramming was the superior method for the replacement of
these drainage pipes," said Guth. "Not only were we able to keep
train traffic moving without any disruption, but we had no fear
of loss of integrity to the rail bed and embankment. We didn't
have to worry about creating any voids during the installation - since
we were driving a solid steel pipe - or any post-project settlement.
Despite the higher up-front costs, it accomplished what no other
method could have."
Liotti and
his crews know about putting holes in the ground. They've used
a variety of tunneling methods for the past 16 years, working
with auger-boring machines, micro-tunneling, hand tunneling
and, more recently, pneumatic pipe rammers. According to Liotti,
pipe ramming has become his preferred method for culvert replacement
work. "When you have soil conditions like those underneath these
rail beds including: like boulders, cobble, sand and gravel,
rip rap and rail ties - pipe ramming with the large pneumatic
tools is much better than traditional auger boring. When we ram,
the lead-reinforced pipe edge shears the ties and cuts and breaks
up the rocks. With auger boring, not only would the boulders
cause the pipe to go off line and grade, but the rocks would
get stuck in the flighting."
Two of the
five culvert replacements demonstrated the reason why Midwest
Mole, Inc. employed pipe ramming. On the first of the replacements,
the crew installed 50 feet of 36-inch pipe. Rather than punch
a new hole through the rail bed, the crew went through the
existing culvert, swallowing up the existing deteriorated 24-inch
corrugated pipe. David Miller, Midwest Mole's crew foreman,
described the installation. "Because
we took the casing over the existing corrugated pipe, we were
able to follow established drainage patterns and didn't have
to fill in the old line with grout and move over for a whole
new line. During the ramming part of the job, the 16-inch HammerHead
Mole hammered the 50 feet in a half hour, chewing right through
old rail ties. If we had been using any other method, those
rail ties would have stopped us cold."
The process Midwest Mole's crew used entailed getting access
to adjacent property and moving its excavation equipment and
the rammers to the site. After excavating the launch pit, they
leveled it and installed their auger-boring unit track and set
it on their desired grade. They had their pipe contractor fabricate
a reinforced soil shoe on the lead pipe so that they had quarter-inch
clearance from the bore wall on the outside of the pipe and a
quarter-inch clearance from the spoil accumulation on the inside
of the pipe. Because of the short length of the bore, Miller
and his crew did not add lubrication for the ramming. After ramming,
they cleaned out the spoil using their auger flighting. All the
restoration work was completed before the crew moved on to the
next culvert replacement.
As the crew worked, the trains ran uninterrupted. The crew did
stop the pneumatic tool ramming once, however, so that the vibration
of a passing train would not shake the track.
Another casing rammed in was 48-inches in diameter in order
to concentrically swallow up the deteriorated 36-inch corrugated
pipe. Midwest Mole brought in the 23-inch HammerHead Mole to
hammer the half-inch wall pipe through the 50 feet of Indiana
limestone to move the new drainage pipe through the existing
culvert.
With its 48-inch adapter ring and 24-inch collets to accommodate
the tool, the HammerHead was lowered into the launch pit some
20 feet below the track surface. The tool was started up; it
taper-locked itself into the collets and the push was on.
"If we had not pipe-rammed this culvert, we would have had to
open a new culvert, direct the creek away from the original channel
and turn the creek on the other side another 90 degrees so they
would meet up," said Liotti. "By hammering with the pneumatic
tool, we saved a lot of time and tons of rip rap that we would
have had to restore the site with." The 23-inch HammerHead pounded
the 50 feet of 48-inch diameter pipe in under 90 minutes, with
most of the time spent during the last 12 feet of the push. When
the crew cleaned out the limestone spoil, they saw the aggressive
chipping accomplished by the tool.
"With pipe
ramming we had no interruption of service," said
Guth. "So we know this is the way to go on these culvert replacements.
There was no appearance of any settlement or any concern about
rail bed or track integrity."
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