The
crew dug the launch pit on a Wednesday, preparing for what
would be a 50-foot push by the time they arrived at on the
other side of the tracks. The bottom of the launch pit was
12 feet lower than the train tracks. Shored with trench boxes,
it was carefully graded to the municipalitys specifications.
According
to Mike Gauger, field superintendent for Globe Contractors
Inc., it was a minimum grade. The pitch for this forced-water
main was 5/10 over a 100-foot run. They wanted it to go up
just a little bit to help keep the air out of the water main
as it went to the hydrant. We graded the launch pit so the
casing was 5/10 lower than the flow line of the pipe, placing
it in the middle of the casing. If the casing rose a bit during
ramming, I had that amount of leeway.
Prior to bringing the first 34-foot casing to the job site and setting it on
a steel I-beam, they brought it to Globes shop and welded a fabricated
soil shoe onto the leading edge. The outside diameter of the soil shoe
was thicker than the outside diameter of the pipe. This lessened the anticipated
friction between the casing and the earth.
The crew
set the HammerHead Mole into the adapter ring and collets the
next morning. They rammed in 28 feet of the casing into the
gray sandy clay until the late afternoon darkness of January
called a halt to production. In the beginning, the 12-inch
HammerHead Mole pushed the casing quite easily into this softer
clay, described Robert Olson, Treasurer of Globe, on
the first days productivity. We were getting three
feet every 15 minutes at first. In fact, we pushed in the first
25 feet with no problem at all.
As the large
casing entered the earth, there was increasingly higher drag
on the outside of the casing from the 42-inch-wide circumference.
The spoil inside the casing drags the pace down. Gauger explained
that his crew anticipated the reduction in ramming speed. In
addition to the outside and inside drag factor, we also knew
the spoil inside a large casing was going to add weight from
the loads of dirt piling up inside the pipe. We knew we would
spend time moving the spoil out, long before the end of the
push.
The next
day, the crew hand-mined out 12 feet of the casings spoil
with air spades; the tunnel being ventilated and monitored
for proper oxygen. Then, they welded on the second 18-foot
section of the casing and resumed ramming at the rate of 2.5
feet every 15 minutes.
We
pushed the pipe past MCIs fiber-optic line which we had
located under four feet of cover. continued Gauger. Once
we got to that point, we dug our exit pit so that we wouldnt
be pushing the bank away from the railroad track.
With the
remainder of the spoil hand-mined, the crew installed the 24-inch
ductile iron water main, and according to the specifications
in the job, poured cellular concrete around the entire annular
space in the casing around the water main to hold it tight
in place and completely fill the void in the 42-inch casing.
Gauger explained, The city of Oak Creek didnt want
any vibration from the railroads to move this water pipe. In
addition, to protect the water line, this concrete grouting
prevented any loss of support to the rail lines. It served
both parties interest.
Robert Olson
recapped his crews experience ramming such a large casing
size,Someone else might have auger-bored this job, another
might have used a larger pneumatic tool. But this tools
ramming time was 10 hours total, and for this size tool, we
thought it did pretty well. Every method has its place. Were
getting our required productivity from this one.
Written by:
Richard A. Yach - Des Moines, Iowa
Provided by: Vermeer Manufacturing Company - Pella, Iowa
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